Yesterday, Mikhaila finally had a day off from work, so we went out to work on Scarlett. I told her the primary goal was to get her engine running, and that we needed to borrow some stuff from Ringo in order to make that happen. With me directing and her turning the wrenches, we removed the carburetors and linkage as an assembly and bolted them onto Scarlett’s engine. After transplanting the battery and rigging up a gravity feed for filling the carbs with fuel, we were ready to go. First check was dwell. I hooked up the meter and had Mikhaila turn the key to on and energize the purple wire to get the engine to turn. It took a few tweaks of the points, but I was finally able to get the meter to point at 32 degrees. Next, we rotated the crank until the groove on the balancer was lined up with 8 degrees on the engine block scale. With the timing light now connected, we twisted the distributor trying to get a spark, but were unsuccessful, so I had Mikhaila aim the timing light with the engine spinning by the starter and we turned the distributor until we could get the groove to show anywhere on the scale. With the timing somewhere within reason, I poured a little gas down each carb’s throat and had Mikhaila start the starter cranking. It took a few tries, but we finally got the engine to fire and run. The strange thing was, that even after twenty-plus years of sitting, there was no lifter clatter and not a whole lot of smoke. We went through a few refills of fuel before calling the exercise a success and I Mikhaila out to the driveway to clean engine shroud pieces while I did a compression check on each of the six cylinders.
Last October we did the same test on the engine and came up with the following results: one @ 160 psi, three @ 150 psi, one @ 120 psi, and one @ 60 psi. This time, with engine warmed up, testing showed two @ 140, one @ 135, two @ 130 and cylinder number two at 45. I squirted some oil down in the spark plug hole and did another check. It went up to 60, so there are still issues. All-in-all, though, the test run was a success since nothing banged, clattered, or untowardly spewed fire. My next move on this will be pulling the left valve cover and checking the rocker arm adjustment on the two valves to that cylinder.
#1
#3
#5
#2
#4
#6
The testing complete, I returned the carburetors and battery to Ringo’s engine compartment. By this point, Mikhaila had finished separating the engine seal retainers from the shrouds, so I released her from working. I, however, still had another project to attend to – this one on Ringo’s distributor. When I’d previously checked the dwell, I’d noticed that it would change with the revving of the engine. In my experience, this indicates a loose pivot pin on the points’ plate. At that time, I’d just plugged the vacuum hose, verified the dwell was holding steady at 32 degrees and moved on. Yesterday, I decided to replace the points’ plate with one that I had removed from Glinda when I’d installed the Ignitor II ignition system a few months back. After the swap, I hooked up the dwell meter, set the dwell to 32 degrees, hooked up the vacuum line, and fired the engine. It would start, but barely and wouldn’t idle. It took me a few minutes to discover my error – I’d neglected to tighten the fitting where the fuel line enters the fuel pump. Sucking air was never going to re-fill the carburetor bowls. With the fitting tight, it only took a few cranks of the engine to get gas in the carbs and the engine running smoothly. Sadly, the dwell still wouldn’t sit still as I revved the engine, so it looks like the distributor shaft bushing gets put on the list for replacement. With a golf tee securely plugging the vacuum hose, I checked the timing – still sitting at 12 degrees BTDC.
At that point I called it a day, put away the tools, and locked up the garage.
Wednesday, December 30, 2015
Tuesday, December 22, 2015
A Short Post
Last evening after faithfully getting me home from work, I rewarded Ringo with a carb tweak. Frustrated that the choke wouldn’t open all the way even after freeway jaunts, I finally broke down and did something about it. I pulled the to-be-mounted tire from his trunk, tossed it into the temporary garage, yanked the spare tire from the engine compartment and rolled it into the trunk. With it out of the way and the engine still up to temp, I removed the right side air cleaner assembly and disconnected the choke rod from the carb. About four twists out and the end of the rod lined up with the carb linkage with the choke wide open. I still need to replace the thermostat on the left side, but at least, once hot, both carbs are fully un-choked.
Thursday, December 17, 2015
Time for an Update
It’s been a while, and, fortunately, nothing very noteworthy has happened in the month or so since I last posted. I’ve been switching back-and-forth driving Glinda one day, Ringo the next. Last Friday evening, after struggling to see though the foggy windshield during my drive in the rain, I decided to spend some time on Ringo addressing his defroster/heater and some other niggling issues. First on the list was adjusting the latch plate on the driver’s door again. A little adjustment out, and latching was again accomplished without slamming.
Moving on to adjusting the idle speed of the engine, I connected the dwell meter to the coil terminal and ground to read rpm. The meter’s switch was set to dwell and I noticed the dwell changing as I blipped the throttle. Hmmm. Off came the vacuum advance hose, and subsequent blipping showed no movement in dwell. Unfortunately, the dwell was off by a few degrees, so I had to adjust that back to around 32 degrees, but not until I’d plugged the vacuum hose with a golf tee. Once the dwell was to spec., I readjusted the timing to about 12 degrees BTDC. Finally, I could give the idle screws a few tweaks to bring the idle speed to a little over 500 rpm with the transmission in Drive.
Next on the list was heater/defroster. I climbed under the dash, removed the three retaining screws, and dropped the controls so I could make sure all the levers were unbroken and properly set. They weren’t. The air one was bent (didn’t need it anyway), the heater one was pulled from its bracket, and one of the two defroster cable ends was also out of place. Knowing the cable was actually seized and that I was going to adjust the heater at the flapper under car, I left the heater one alone, but did re-seat the misplaced defroster. Turning my attention to the defroster doors in the rocker tunnels, I checked their operation and they were good-to-go.
Once I backed the car up on the ramps, I blocked the front wheels and released the parking brake. With 7/16ths and ½ inch wrenches in hand, I slid under the lifted rear and pushed the heater box door wide open. Next, I tightened the parking brake cable nut a half-dozen turns or so.
By that time it was late, so I called it a day.
Monday and Tuesday were Glinda days, but yesterday morning I grabbed Ringo’s keys and slid behind his wheel for my morning drive. I noticed, as I accelerated to get on the beltway, that the throttle response was not a good as the last time I’d driven him. Looks like I need to bump up the timing. Today he again was my chosen whip, and, while I could still stay up with 65-70 mph traffic, I wasn’t happy with the loping at part throttle. I’ll also be checking dwell and looking for vacuum leaks the next time I’m under his engine lid.
Moving on to adjusting the idle speed of the engine, I connected the dwell meter to the coil terminal and ground to read rpm. The meter’s switch was set to dwell and I noticed the dwell changing as I blipped the throttle. Hmmm. Off came the vacuum advance hose, and subsequent blipping showed no movement in dwell. Unfortunately, the dwell was off by a few degrees, so I had to adjust that back to around 32 degrees, but not until I’d plugged the vacuum hose with a golf tee. Once the dwell was to spec., I readjusted the timing to about 12 degrees BTDC. Finally, I could give the idle screws a few tweaks to bring the idle speed to a little over 500 rpm with the transmission in Drive.
Next on the list was heater/defroster. I climbed under the dash, removed the three retaining screws, and dropped the controls so I could make sure all the levers were unbroken and properly set. They weren’t. The air one was bent (didn’t need it anyway), the heater one was pulled from its bracket, and one of the two defroster cable ends was also out of place. Knowing the cable was actually seized and that I was going to adjust the heater at the flapper under car, I left the heater one alone, but did re-seat the misplaced defroster. Turning my attention to the defroster doors in the rocker tunnels, I checked their operation and they were good-to-go.
Once I backed the car up on the ramps, I blocked the front wheels and released the parking brake. With 7/16ths and ½ inch wrenches in hand, I slid under the lifted rear and pushed the heater box door wide open. Next, I tightened the parking brake cable nut a half-dozen turns or so.
By that time it was late, so I called it a day.
Monday and Tuesday were Glinda days, but yesterday morning I grabbed Ringo’s keys and slid behind his wheel for my morning drive. I noticed, as I accelerated to get on the beltway, that the throttle response was not a good as the last time I’d driven him. Looks like I need to bump up the timing. Today he again was my chosen whip, and, while I could still stay up with 65-70 mph traffic, I wasn’t happy with the loping at part throttle. I’ll also be checking dwell and looking for vacuum leaks the next time I’m under his engine lid.
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